So I did a few checks to make sure there would be enough space between the swing arm structure and the middle spacer for the grease to be able to be pumped along the shaft to reach the needle rollers at each end. Everything checked out OK.
I did not know how thick the swing arm housing would be and thought if it was too thin to thread for the grease nipple then I would need to weld a nut on the outer surface of the swing arm. I need not have worried as the thickness of the metal was about 1/8". Plenty to cut a thread in with my 6mm tap for the grease nipple.
Tapped the hole, threaded the nipple in and all ready to go. Just waiting on the needle rollers and spacers to arrive to complete the job.
The real bonus here is the swing arm filled with grease will keep any water out. As my whole problem of wonky rear end handling came about because this cavity in the swing arm had filled with water and everything had rusted.
See photos attached:

I am pretty sure anyway.
Oh well, I guess I'll have to get it next time. I put PLENTY of nice clean grease in there when I put things back together though. My Yammies have a zerk on the drilled pivot bolt which works REAL well.
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