I thought that maybe the ebay head valves weren't sealing, so I got the original machined, put it back together with new gaskets, no difference.
It's not the carbs - I have two pairs, both are properly cleaned/new O-rings and one pair I know to be good. Same response on both.
I have UNI Pods and shorty exhaust, have tried wide variety of jet/needle settings and the behavior is pretty much the same.
I thought maybe I was setting the timing incorrectly. I've triple checked it twice and even opened up my other engine to compare. Everything checks out.
Could this be explained by a bad piston ring? Seems unlikely to me considering the low miles. Could it be something in the bottom end?
Here's a video with the original head back on and me demonstrating the L/R behavior.
https://www.flickr.com/photos/976376.../shares/W12TK8
Timing:



TIA!
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