The intake all seems to be tight, but maybe the filter gasket could be a little better, but there is a gasket there, I know that's not causing the noise , but I thought maybe that was why it was sluggish.
I did adjust the valves , and it could be off a bit but I've checked the clearance and it's pretty close.
I also put a used but good stock exhaust back on it, but everything seems tight .
The cam chain also appears to be good , with no slack.
Could a little leak at the exhaust header be the culprit for the noise? Or is it more than likely the valves being out a bit ?And that's why it's a little sluggish too.
I did a compression test and that seems real good ; #1-180 , #2-180 , #3-175 and #4-185 .
Sorry for the novel , but I'm stumped , any thoughts from the experts?
, I did a rebuild but didn't change the jets but I did clean them. I did replace the float valves and seats though and all of the seals. My rebuild kits were made by Tour Max , made in Japan. As far as I know everything in the carbs were stock befoer I took them apart and I didn't mess with the air mixture or change the jets. Big T how do you suggest that I seal the headers at the heads ? Can I use the high heat sealant ?
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