The carb boot pipes and O-rings are new, but the airbox side boots were hard and shrunk up a little so the decision was made to replace them.
Took the bike out yesterday for a longer ride (post repair) and the hanging idle is gone. Also, the temp gauge hovered in the 250 F range. Still hot, but 50 F lower than before.
Going to pull the plugs and check color next, but the bike runs flawlessly so I don't expect to see much. Actually, the bike ran fine at freeway speeds even with the airleak, only it was obviously running lean. Guess that goes to show, don't judge your mixture by how well the bike runs. For you guys running pods or a modified exhaust, better double check your mixture otherwise you could be cooking your engine needlessly. And for guys with a stock intake system, airbox leaks are almost as bad as intake boot pipe leaks.
Gotta pay attention to details.
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