Very pliable head to carb boots with new O-rings.
Stock air box with new OEM oiled filter
Stock exhaust
New O-rings on the needle jet tubes that were removed from the bowls and cleaned
Stock 115 main and 17.5 pilot jets
9,300 mile one owner bike with 130psi a side compression
Carbs were cleaned and dissembled up to the point of removing the butterflies and shaft.
The mix screws also have new O-rings and seem to have little affect with setting from 1 to 3 turns out.
Motor runs hard all the way to 9,000 on the road but when it has a 6-7 miles of warm up wants to hang around 3,000-4,000 RPM
Is running for sure lean and the plugs show it , no cable hang ups or choke enricher plunger issues.
Were do I go from here ?????????????
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