If you've been following along I've went through the carbs, done all the suggested cleaning plus some, and replaced everything. The valves are in spec and the carbs sync'ed.
After settling on a 150 mikuni main jet and leaving my needle at 4 my last thing was to try going up with the pilot jet to get some adjustability on the screws. After putting in the 40's I really didn't notice the difference in idle that I was hoping for. If anything I ended up turning out an additional 1/4 turn past 3, which is where I had it set through main jet tuning. 3.5 turns out had smoke coming out the exhaust when rev'ed (too rich). Either I need to go up more on the pilot, and I'm thinking at least two steps, or something else is wrong.
I decided to record what how the idle behaves after a good long flog last night. The temps were in the 90's by the way.
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