Sunday night I got down under the seat and air filter to the connector behind the R/R unit. It was wrapped up solid in electrical tape. When I cut it free, I found the connector had been partially melted, bare wires and a whole lot of black silicone applied to hold it all together. What a mess. I have attached pictures.

It is incredible to me how this bike was functioning almost flawlessly, even with this going on. A failure at this plug would have been not only inconvenient, but probably costly as well.
I have re-done all connections properly, and am currently topping up the battery prior to running a complete diagnostic on the charging system.
Lesson learned. I should have checked it earlier, but fortunately no harm done this time.
. If you dont get a solid 14-14.5 vdc above 2k its time to call Duane.
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