I have never done a tear down before, but I think the carb looks pretty good thus far. The float bowl gasket was barely dirty, someone may have checked the float bowls recently, the gasket looks almost brand new. The float bowl screws were easy to remove, much to my happiness as others were a straight PITA.
Bad news though..
Have a big problem though... I THINK I may have stripped the pilot jet. I removed the rubber plug, which is in good condition, loaded the slot with wd-40 and carb cleaner, and waited 2 minutes. Stuck in my crafstman screw driver and proceeded to turn, it slipped pretty bad two times. So I stopped peered in and it looks to be stripped a bit. UH OH. So I loaded it up again with wd-40 and am taking a break...
I will post pics later of the carb to the point I am now.






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