Martin (Brit 7.11) suggested a "leak down test", so I built a leak down tester using some (new old stock) air fork kits I had in a box for the air valve and guage. Anyway, the thing works, I used an old S&W syringe type pump to pump in 30 psi, and after 5 minutes there was no loss of pressure at all, but after an hour it was down to 15 psi.
I think Martin suggested to listen to where the air is escaping, but I couldn't hear anything, and I guess the leak is that slow that I wouldn't anyway. I tried brushing a little liquid detergent around the head gasket joint to watch for bubbles, but couldn't see any. Does anyone know where I should go from here? I tried re-torqueing the head down, but it made no difference at all, so I guess the head has to come back off, so I can pay more attention to the joint faces, boo hoo.
If you'd like to see the leak down tester I built, email me at sherriffbuck@yahoo.com and I'll send you some pics.
Comment