New rings & honed bore 1500 miles ago. New head gasket. Valves lapped & checked for leaks with gasoline. Compression is 150/143/150/145 hot WOT.
It is down on power, especially at high revs. It does 100 but takes a while to get there. I've checked the cam timing twice, the valve clearances three times, and the spark timing once. The plugs all look okay. I put in a new Suzuki air filter today. I have checked the jets twice to make sure I put the bigger mains in #2 and #3. The slides move very smoothly. The rubber airbox tubes are fairly new. I also put compressed air into it through the breather tube and sprayed the tubes with soap: no bubbles. I also sprayed the exhaust with soapy water: no bubbles. (I also felt for a leak.) I checked the float height last August.
I don't know what else to do. I don't want to say how I ran in the motor, because no matter which way I did it, half of you will have strong opinions that I did it wrong.

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