I was able to get the Twin Balance Carb Syncher on Cyl 1 & 4 and they were close. I will be pulling the Carbs of tonight; what's your opinion on the next step. 1) Bench synch with a Gage Pins slid under the throttle valves or 2) Since the 2.0 Slide Cutaway allows more air than the 1.5 Slide they replaced is the Pilot jet now to small to let my GS1000 idle? Sudco recommends a Pilot Jet of 25 but that's at sea level (See below) The intake boots & O-rings are okay. I believe I have check Step 1 & bump the pilot because it flat refused to run without a liberal dose of choke.
Mikuni VM29 S/B Configuration:
Pilot: 15
Needle: 5DL31-2
Main: 127.5
Air Screw: 1 turn out
79 GS1000: Wiseco 1085 10.25cr Compression sound
Andrews S-1
K&N Pods
Supertrapp 4 into 1
Altitude: Denver, CO. 5150 Feet
. That's the current status. After doing some additional reading on the Forum, I believe my Dyna Coils would also benefit from the Coil Relay modification.
. Yesterday I did change the pilot jets from a set of 20's to 22.5's and set the air screws at 1 full turn out. I want to get that air screw setting at 1 full turn, so I achieve +/- idle mixture leeway. I will probably have to wait till this weekend to perform WOT plug chops.
Next I headed back out to Rocky Flats and maintained throttle @ 5000 rpm for 1 mile. I had no issues with surging but the plugs in cylinders 1 & 4 were actually whitter than the day before. This is probably because I didn't maintain 4500 rpm for 1 mile on the previous day or at least I believe that's plausable. All these plug chops were performed with B7Es's, so since I just received my latest Z-1 order of VM25 pilot jets I will be installing a set of B8ES's and will recheck this week and than hopefully move onto the main. I believe the coil relay modification (thanks guys) bolstered the performance of the green Dyna Coils & Accel 8.8 wires but that just a seat of the pants opinion. More later . . .

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