After tons of dyno time I just cant get rid of a big hole in the mids.
I think its the porting job and 38mm Mukuni RS's that are causing an over carburation/bad mids effect.
Its fine from 0-4000, majorly bad (you should see the dyno chart) 4-6500, Strong after.
Ive got a spare brand new head (still in the box) and have been thinking of just going back to a stock head and new valves but still running the not overly high lift webcams and putting the original (New Zealand Wire Wheel spec) 36mm roundslide mukunis back on.
Anyone else been through the same...???
BTW, Everything is set right.
The bad mids cant be dialed out so it has to be the head/carb combo....
By all accounts from what ive been told by people, The 38s are just to big unless youve got a seriously big engine with a really good port job.
For street use they are a bit of a joke cause they are the equivalent of putting 44mm CV's on which is ludicrous.....But I was young and stupid;-)
HELP!!

, I was real careful about that detail, Unlike some people I know with monoshocks etc :roll:
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