Anyway I ran another Compression Test and and all 4 cyclinders are 115 - 120 PSI so thats a good improvement. Not ideal but should be enough to fire up.
And it goes. Pretty rough and smokey but considering how many years it has been i am very satisfied.
I have a video but cant upload to IMGBB website so you will have to believe me.
Everything is connected up temporarily
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[/IMG]While i had the engine apart i also discovered that it is now 1199cc so along with the RS36 carbs that would have been 1 exciting beach racer motorcross bike in its previous life.
Now to get it road worthy. First item to repair is the front fender which is held together with duct tape
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[/IMG]A bit of fibreglass on the underside
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[/IMG]And it is now in 1 piece
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