I finally pulled apart the (?)Two Brothers can on the 4-into-1 system on my 1979 GS 1000 that I repacked when I was first bringing the bike back to life. The good news was that all of the stainless-steel wool packing that I put in was still there. The bike was still too loud; it had a straight-through baffle, and I fabricated a cap so the baffle isn't so "straight-through" any more. I can feel that the power has moved lower in the rpms. The bike has K&N pods, the 4-into-1, and DJ Stage 3 jetting. I haven't had a chance to really wring out how the carbs feel, but they don't seem too bad. Any thoughts on if I might to need to rejet at least the pilot circuits, or if I can just lean the mixture with the air screws on the VM 26s? I've been planning on shimming the needles as there is a lag when rolling on the throttle below 3k, and I'd like to sharpen that up.
