G
G0FHM
Guest
Where are the pilot screws set?
2.5 turns, as stated as a starting point in the rebuild "howto"
Did you remove the pilot jets and hold them up to a light to make sure they are open?
Yes - And have blasted carb cleaner through them.
Did you spray carb cleaner though the choke pick up tube and make sure it comes out the choke plunger passage?
Yes
Did you make sure the choke tube passage in the float bowl is open?
Yes - Again, blasted with carb cleaner, and got a face full in the process!!
Did you adjust the engine valves (not likely the problem, but part of basic maintenance)?
All within tolerance!
Did you look though the Newbie Mistakes thread to make sure you are avoiding the common problems?
Yup!
Did you go though the entire carb rebuild tutorial and replace all O-rings, including those on the intake boots?
Yes!
Seems pretty obvious the problem is fuel related, since as you said there is spark (although you should verify the plug in the cylinder is firing). I suggest going back to basics and verifying each step in the process.
It's not the plug, I've swapped them between pots and it's still #4 that is inoperative. I've had brand new Bosch & Delco plugs fail before now - But i've never had an NGK let go on me... Yet!
The only conceivable thing left, is the seal between the intake stub and head. I've tested the inlet stub (don't ask me how!), and that doesn't leak.
I did fit new O rings, and the ring wasn't a very good fit within the groove - And I'm just wondering if it sprang out when I offered it up to the head, although on inspection it shows no signs of being pinched. I'll stick it in place with a smidge of silicon RTV when I put it back on, which will also help the seal.
If that is indeed the problem, then it hid itself very well. Normally a bit of rubber fuel hose stuck in the ear makes an excellent makeshift stethoscope, and I've successfully found leaks using that method many times over the years.
One thing I did find, was the revs were very slow to recover after being raised. Lubricating the advance mechanism (it was quite stiff) helped a little, but didn't totally stop the problem. That is consistent with a vacuum leak.
I'll put it all back together tomorrow and report back!
Thanks,
J