G
Guest
Guest
So I have completed tuning for main and needle on my UNi podded 83 750.
If you've been following along I've went through the carbs, done all the suggested cleaning plus some, and replaced everything. The valves are in spec and the carbs sync'ed.
After settling on a 150 mikuni main jet and leaving my needle at 4 my last thing was to try going up with the pilot jet to get some adjustability on the screws. After putting in the 40's I really didn't notice the difference in idle that I was hoping for. If anything I ended up turning out an additional 1/4 turn past 3, which is where I had it set through main jet tuning. 3.5 turns out had smoke coming out the exhaust when rev'ed (too rich). Either I need to go up more on the pilot, and I'm thinking at least two steps, or something else is wrong.
I decided to record what how the idle behaves after a good long flog last night. The temps were in the 90's by the way.
If you've been following along I've went through the carbs, done all the suggested cleaning plus some, and replaced everything. The valves are in spec and the carbs sync'ed.
After settling on a 150 mikuni main jet and leaving my needle at 4 my last thing was to try going up with the pilot jet to get some adjustability on the screws. After putting in the 40's I really didn't notice the difference in idle that I was hoping for. If anything I ended up turning out an additional 1/4 turn past 3, which is where I had it set through main jet tuning. 3.5 turns out had smoke coming out the exhaust when rev'ed (too rich). Either I need to go up more on the pilot, and I'm thinking at least two steps, or something else is wrong.
I decided to record what how the idle behaves after a good long flog last night. The temps were in the 90's by the way.

