J
Jason the terminator
Guest
It started out trying to get my carbs jetted properly. I ordered a Dynojet kit, K&N pods and a Marving exhaust to replace the V&H 4to1 (so I would have a few more inches of ground clearance).
The PO had installed the V&H and jetted it by putting a 160 pilot air jet, 47.5 pilot jet, 125 mains. It would pop on decel indicating a lean condition.
I installed the Dynajet kit per instructions. Drilled the slides, 138 main, needle 3rd notch down, floats 22.4mm, 2 1/2 turns out on mixture screw, 160 pilot air jets cause I did not have the 170s. A bench sync was done also. I tried to get it to run with no luck. Checked the spark and it was week so I did a coil relay mod. Still could not get it to run properly.
Got a hold of Rustybronco to ask some questions and he offered to come over and give me a hand. After many hours trying to get it running he said I need to get the stock air pilot jets(170) and it was still blowing the spark out. So I investigated and bad signal generator and the ignitor was not testing good per manual.
Now we are into riding season so I was not going to mess around and try and figure out a 30 electrical system. I just order the 170 pilot air jets and a Dyna 2000 kit. When I received them I installed figuring that my problems were solved but they are far from it.
The pilot system is to rich. At 2 turns on the mixture screws at idle it will fowl the plugs in about 30 sec. After some phone calls with Rapidray and Rustybronco today here is where I am at. With 1 turn out, no pod filters and wet float height at 7.5mm it will idle and rev but has a flat spot at 2-5000rpm. It still seems on the rich side still.
The bike only has 6k original miles on it and all the parts that I listed were purchased new. The only thing that I am wondering about is that it looks like the valve cover was removed and wonder if the PO degreed the cams. If so could this add to my issues?
The PO had installed the V&H and jetted it by putting a 160 pilot air jet, 47.5 pilot jet, 125 mains. It would pop on decel indicating a lean condition.
I installed the Dynajet kit per instructions. Drilled the slides, 138 main, needle 3rd notch down, floats 22.4mm, 2 1/2 turns out on mixture screw, 160 pilot air jets cause I did not have the 170s. A bench sync was done also. I tried to get it to run with no luck. Checked the spark and it was week so I did a coil relay mod. Still could not get it to run properly.
Got a hold of Rustybronco to ask some questions and he offered to come over and give me a hand. After many hours trying to get it running he said I need to get the stock air pilot jets(170) and it was still blowing the spark out. So I investigated and bad signal generator and the ignitor was not testing good per manual.
Now we are into riding season so I was not going to mess around and try and figure out a 30 electrical system. I just order the 170 pilot air jets and a Dyna 2000 kit. When I received them I installed figuring that my problems were solved but they are far from it.
The pilot system is to rich. At 2 turns on the mixture screws at idle it will fowl the plugs in about 30 sec. After some phone calls with Rapidray and Rustybronco today here is where I am at. With 1 turn out, no pod filters and wet float height at 7.5mm it will idle and rev but has a flat spot at 2-5000rpm. It still seems on the rich side still.
The bike only has 6k original miles on it and all the parts that I listed were purchased new. The only thing that I am wondering about is that it looks like the valve cover was removed and wonder if the PO degreed the cams. If so could this add to my issues?