Float level clarification.
Thank you hikermike & nert. I try to walk the thin line between going on & on or not giving enough detail on a sort of long running & detailed issue.
Don't think you need to replace choke seals and plungers, just make sure they are closing and seating all the way.
Carbs are very clean & no signs of corrosion, all plungers move freely & seem to close fully with sufficient slack in choke cable when closed.
Yes i know choke would worsen a rich mixture, but, have you tried it to totally eliminate the possibility?
I could try to test the seal of the plungers with some slight air pressure. Will look into this.
We don't know your tech level, so be patient with our questions.
I often face that question my self. I work at Suzuki/Honda shop with 2 pretty sharp oldtimers who try to guide me through this. I am a slow worker, especially on my own bike.
How long have you had the bike?
Well 1981 GS850G, owned since about 2003. Had at least 20k on it then now proably over 50k. (several instances of speedo cable, drive breakage and replaced speedo/tach with nice used unit some years back) PO seems to have left it out in the weather. Someone had already been into the engine before me, not too gentle either. Had to helicoil several threads for the camshaft caps.
How long have you had the problem?
Some years back was running a bit lean tho ran well seat of pants. Last fall tried to go up one step on mains & pilots to get more color in plugs. Ran crappy & very rich. Went back to stock mains and later stock pilots (115/40) but could not loose the rich running. STRANGE, NO?
Over time things deteriorated in smooth running & compression tests & leak down test indicated most cylinders had both ring & valve issues. Confirmed when torn down including # 2 exhaust valve burnt with some cracks & seat shot.
New pistons, rings, cylinder honed(measured & no bore needed) valve replaced, seat cut, valves lapped & checked, new valve springs all around.
Restored the stock foam air filter from previous K&N. Started with mixture screws out 2 turns but too rich, kept cleaning plugs & setting screws leaner, replaced K&N to help lean out. As engine breaks in it runs better & better & stronger but prob still there once warm at idle with cutting out unless 1300-1500 & previously stated gas guzzling & sooty in the plugs.
Had checked the possible vacuum fuel valve leak possibility. Nothing there, but as always will recheck again. Believe that would show up on #2 cylinder only tho,...no?
Am in the midst of checking the coils as to resistance readings. Initially primary reading looks ok. Will check rest next night or two. Took off tonite to watch America's Got Talent. Wish I did so use them as surrogates as I can't sing, dance, ride a bicycle, do magic etc.
Your questions are great, please excuse my answers. You have given me ideas & homework.
Thanks again so much,
DH