Keith,
Thanks for your dedication here to my problem! Answers as follows:
4 into 1 pipe: It had a Vance & Hines on it until about a year ago. It rotted out and I replaced it with a Mac canister type. When I did, there were no drivability changes- only a different sound.
Filter Mods: The bike has never had a air box cover since I got it. I've been looking for one for about two years- whenever an air box comes on e-bay, it seems the filter box is not included, just the big air box. I have fabricated a cover that is a small frame with wire mesh screen. I've also run the bike with no filter at all (taboo, I know) with no changes in drivability at all. The actual filter is a single UNI foam type filter.
Choke: The choke does nothing to help start the bike, and at any time while running- hot or cold- any choke will kill the bike immediately. Even 2mm of pull on the knob and the bike will cough and die.
Jet sizes: The rebuild kits I bought includes jets to bring it to stock. There are two to chose from, 107 and 112.5.
Mixture Screws: All the old cracked, broken o-rings came out when I cleaned the carbs in the spring. I also made sure these holes were clean when I worked on them last weekend.
The plugs I have in there are about 2 months old. I gapped them and rode for a while and did a plug read. All of them looked pretty good, maybe a little more white than I would like to see, but not super bright white. I still haven't gotten a chance to pull the plugs since this latest problem, I'll do that tonight. With the mixture screws, The highest idle seems to be at about 5-7 turns out- much more than everyone seems to be right. I'll play with it a little more tonight, and let you know what I come up with.
The jets in right now are 125's, I'm sure the last guy jetted for the V & H pipe that was on it. As I understand, the MAC canister is a little more restrictive. Think I should put the stock 107's or 112.5's in and try them? Keep in mind that when I put the MAC on a year ago it ran ok. It wasn't till last weekend when I replaced the mixture screws and needle jets, did I have a problem.
Thanks again!
Thanks for your dedication here to my problem! Answers as follows:
4 into 1 pipe: It had a Vance & Hines on it until about a year ago. It rotted out and I replaced it with a Mac canister type. When I did, there were no drivability changes- only a different sound.
Filter Mods: The bike has never had a air box cover since I got it. I've been looking for one for about two years- whenever an air box comes on e-bay, it seems the filter box is not included, just the big air box. I have fabricated a cover that is a small frame with wire mesh screen. I've also run the bike with no filter at all (taboo, I know) with no changes in drivability at all. The actual filter is a single UNI foam type filter.
Choke: The choke does nothing to help start the bike, and at any time while running- hot or cold- any choke will kill the bike immediately. Even 2mm of pull on the knob and the bike will cough and die.
Jet sizes: The rebuild kits I bought includes jets to bring it to stock. There are two to chose from, 107 and 112.5.
Mixture Screws: All the old cracked, broken o-rings came out when I cleaned the carbs in the spring. I also made sure these holes were clean when I worked on them last weekend.
The plugs I have in there are about 2 months old. I gapped them and rode for a while and did a plug read. All of them looked pretty good, maybe a little more white than I would like to see, but not super bright white. I still haven't gotten a chance to pull the plugs since this latest problem, I'll do that tonight. With the mixture screws, The highest idle seems to be at about 5-7 turns out- much more than everyone seems to be right. I'll play with it a little more tonight, and let you know what I come up with.
The jets in right now are 125's, I'm sure the last guy jetted for the V & H pipe that was on it. As I understand, the MAC canister is a little more restrictive. Think I should put the stock 107's or 112.5's in and try them? Keep in mind that when I put the MAC on a year ago it ran ok. It wasn't till last weekend when I replaced the mixture screws and needle jets, did I have a problem.
Thanks again!