New to me 1982 GS1100 GK. PO changed the main jets to 120. Pilots are stock 40's. Original air box. Delkevik 4 into 1 exhaust with the center baffle removed. All pilot screws are set at 3 turns out using the engine RPM as a guide. The bike starts and idles perfectly and runs really well at mid and WOT but has always had a stutter at 1/8 throttle. Also, the number 2 cylinder is always fouled out. I'll clean the plug and put it back in, and it only takes about a day to foul out again. Also, it smells like gas at idle.
I finally took the carbs apart and to check them and document what was done previously. Everything was really clean and the float heights we all right on. The number two carb bowl had some light sediment in the bowl and the pilot was partially blocked. I was able to clean it out using carb cleaner and compressed air. I did clean all of the passage ways for the main and pilots and made sure the bowls were all spotless. But I did not split the carbs or do any kind of ultrasonic cleaning.
Put it all back together and it ran like a monster. No stuttering at all. But not long after, it started hesitating again at 1/8 throttle. Took the #2 plug out and sure enough, it's black black. Also, all the other plugs are always perfect. It's just the #2 cylinder which seems to be the source of the issue.
My question is, should I just replace the pilot? Should I just dial the #2 pilot back a bit? Or is there somewhere else I should be looking?
I finally took the carbs apart and to check them and document what was done previously. Everything was really clean and the float heights we all right on. The number two carb bowl had some light sediment in the bowl and the pilot was partially blocked. I was able to clean it out using carb cleaner and compressed air. I did clean all of the passage ways for the main and pilots and made sure the bowls were all spotless. But I did not split the carbs or do any kind of ultrasonic cleaning.
Put it all back together and it ran like a monster. No stuttering at all. But not long after, it started hesitating again at 1/8 throttle. Took the #2 plug out and sure enough, it's black black. Also, all the other plugs are always perfect. It's just the #2 cylinder which seems to be the source of the issue.
My question is, should I just replace the pilot? Should I just dial the #2 pilot back a bit? Or is there somewhere else I should be looking?