Kara25
Forum Mentor
Hi guys long time no see! So after putting away my fresh totally rebuild motor with only 200Kms on my garage due to super busy and demanding working conditions 7/7 i finally found some time to go maybe for a little ride. Hooked up my lithium ion battery (had it taken home when i parked and covered the bike in the garage) added 5L of fresh fuel pulled the choke and the beast woke up after super fast and easy! But something was wrong immideatly i could tell that the exhaust note was rough and sounding like a harley than an inline 4. Anyway i started riding away on the neighbourhood but the bike would surge and not pull like it was just 4 months ago. I thought ok pilots got gummed from sitting even though i drained the bowls maybe i will be super lucky and adding some techron later will clear it up. Didnt even tried that. Came to halt cause the bike clearly was struggling and it dawned to my while i was trying to keep it idling to pull the wires of each plug to see if i have electricity on all 4. Pulling No1 NO DIFFERENCE AT ALL. Pulling No4 IMMIDIATELY IT DIED! Ok now thats weird i limp it back home take the tank off and use an old plug on each wire laying on the head. 2&3 super strong and fat spark as long as i keep pressing thr button. 1&4 only a tiny spark the moment i first press the button and then completely dead no matter how long the starter button is pressed! Bike has in the course of the past 3 years in order. 1. Accel supercoils- 3ohm.2.lithium battery.3.New aftermarket ignitor from EU based vintage motorcycle electronics company called Wielctronic.4. Ricks stator DIRECTLY hooked to Ricks lithium ion specific R/R.4 New Arrowhead starter relay . what i managed to figure out was that even though i was running on 2 maybe sometimes 3 pots the battery charged ok during my short ride after pulling out the multimeter to start checking things it showed 13.93V. So i assume stator and R/R are OK. also neasured ohms at coils both show almost 4oms and from 13,9V at the terminals they show 13,2V. I think a 0,7Volt loss is at acceprable limits?? So any thoughts??? Is the <<new>> igniter trash??? Or i need a new Accel coil?? Also tested the signal generator using the method on Clymers and i am getting 73ohms while checking both connections on the generaror side to the ground which is in the ranges the manual states 60-80ohms so pickups are also ok.! What is going on any ideas??
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